CPPA Bleaching Committee
Technical Session, May 7, 1996
1. Seven Steps to Chlorine Freedom
- Murray Walters, Harmac Pacific (see Appendix 3)
- 1100 tpd bleached kraft, 3 lines of everything except recaust
- Motivation
- European market demands
- BC government legislation
- Simplify grade structure (11 grades, depending on Cl2)
- Industrial hygiene (release hazard)
- Constraints
- ClO2 plant capacity
- operating costs
- pulp quality
- Seven process modifications to provide reductions in chlorine dioxide demand
- H2O2 reinforced extraction stages
- 3 kg/UBDt
- 1:1 replacement
- low ROI, but a strategic decision
- D0 stage pH control
- optimum pH near 2.5 before ClO2
- dilute H2SO4
- lab/mill trials to determine the benefit
- projected 10% reduction in kappa factor
- C Bleach prewasher
- > 30 kg/UBDt COD from Chemiwasher (reduced to 5)
- give up Papricycle washer
- projected 5.5 kg/BADt reduction in Do ClO2 usage
- C Bleach medium consistency D0 stage
- new upflow to existing downflow tower
- 40 minutes in upflow alone, 145oF (typically operators run at 60 min, 165oF)
- projected 13% reduction in ClO2 demand
- sequence now DEopDED
- Full time operation of Kamyr line Oxygen Delignification (basically added MgSO4)
- 30% kappa number reduction
- significant strength loss and blending restrictions solved by magnesium sulphate system and C bleach prewasher
- projected 10% reduction in kappa factor in B bleach (at same CEK = 4)
- Mini Oxygen Delignification for Chemiwasher line (650 tpd)
- similar to Kamyr line system
- 30% kappa number reduction
- C bleach prewasher as post-oxygen washer
- commissioning scheduled for November 1996
- A and B Bleach medium consistency D0 stages
- projected 13% reduction in ClO2 demand
- implementation dependant on HPI strategic plan
- Economic Impact
- planned steps 1-5: $2.94 million capital ($6.09)/BADt op cost 61% ROI
- actual steps 1-5: $2.86 million capital ($6.86)/BADt op cost 72% ROI
- Operating Experience
- Positive:
- ClO2 demand reduced to 37 tpd
- upflow/downflow easy to operate
- less vulnerable to BSW upsets
- H2O2 = increased operating flexibility
- fewer grade changes
- Negative
- pH probes require frequent recalibration
- dropleg corrosion
- Conclusions
- ClO2 demand reduced to target level
- chlorine eliminated from bleaching process
- AOX reduced to about 0.4 kg/BADt
- fibre line modernized
- mill operability increased
- operating costs reduced
- attractive economics
2. Interaction of Hydrogen Peroxide and Chlorine Dioxide Stages in ECF Bleaching - Dave Senior, ICI
(paper was presented at 1996 International Pulp Bleaching Conference, Washington - see Appendix 3)
- DEopDPP sequence consistently reached higher brightness than DEopPDP, despite similar chemical charges
- Objectives
- confirm the DP vs PD effect on other pulps
- understand the mechanism
- provide basis for improved bleach sequences
- Literature Search - not much there
- D(EO)D(EP)D = 91.1 ISO vs. D(EOP)DED = 90.2 ISO
- location of Eop stage
- position of (PO) in bleach sequence impacts brightness
- TAPPI Jan/96 - ClO2 before H2O2 improves P stage
- Experimental
- full bleaching of southern softwood
- DP brightness consistently higher than PD
- final brightness was the same, but P1 vs D1 different
- limited bleaching of NBSK (DEPD vs DEDP)
- limited bleaching of hardwood (DEPD vs DEAPD vs DEPAD)
- extraction of lignin, compare 31P-NMRs
- pulps prepared from each stage of bleaching in DE
- theoretical says can predict that peroxide is more efficient after ClO2
- DED pulp consistently lower phenolics and condensed lignin than DEP
- Conclusions
- brightness consistently higher when D stage preceded P stage
- Questions:
- does this 31P-NMR show the tradeoff between ClO2 and peroxide? Maybe
3. Survey Results: Doug Reeve - University of Toronto (see Appendix 3)
1. Substitution of Chlorine Dioxide for Chlorine in Canadian Bleached Chemical Pulp Mills;
2. ECF Practice in Canadian Bleached Kraft Pulp Mills
- Substitution of Chlorine Dioxide
- ECF continues to increase, TCF close to zero
- softwood 1991 vs. 1996: slight change to lower kappa numbers into bleach plant
- hardwood 1991 vs. 1996: more change to lower kappa numbers into bleach plant
- ECF has almost caught up to 50% substitution in 1996 (ECF = those who campaign or are totally ECF)
- nobody using less than 50% substitution
- dominant non-ECF sequence DcEoDED (E1 may have H2O2 )
- dominant ECF sequence DEopDED (E2 may have H2O2 )
- ECF brightness typically 89-90, so no problem getting high brightness on ECF
- ECF Practice in Canada
- Softwood only, 20 conventional pulping, 9 with O2 delignification
- conventional
- most still measure saltcake, not COD, about 5-10 kg
- 28-32 kappa to bleach plant
- 0.20 kappa factor, PEKappa 4.8
- O2 delignified pulp requires more chemical per change in kappa number (as expected, since starting at a lower kappa number)
- How can some mills operate at the bottom of the graphs? These are the benchmarks
- Where is the best place to put your oxidizing power? It depends - not everybody’s plants have the same strengths and weaknesses
- Can we identify the critical parameters that make a mill do well? Not yet. The intention is to present another questionnaire for back end of bleach plant
4. Bleach Washing Evaluation Methods - Rae Cunnington, Dennis Matson
(compendium of six presentations)
- Oxygen delignification washing
- pre-oxygen washing well understood; require sufficient pre-oxygen stage washing to keep below a COD of 25 gpl in liquor from oxygen stage reactor - no viscosity loss at this level
- post-oxygen washing requirements - 2 drum filters generally not enough, need 2 wash presses, or 2 pressure washers, or 2 stages of diffusion washing, or equivalent washing in multi-stage washers to provide low carryover to bleach plant
- Bleach Plant Washing
- requirements not well understood, many mills now looking seriously at the savings that are possible from optimizing bleach plant washing
- Important Wash Parameters
- Norden Number (for definitions see MR291, or the new Pulp Bleaching Principles and Practice text)
- Modified Norden (Ek)
- Displacement Ratio (DR)
- see Appendix 3 for comparison of wash parameters for different types of washers
- What are we trying to do?
- Do - wash out spent hydrochloric acid and some chlorinated dissolved lignin
- Eo - wash out dissolved organic material
- Paprican
- Displacement ratios on a D0 washer for Na, Ca, Mg, Cl, TDS, lignin show lots of variability in efficiency as measured by displacement ratio
- Ca and Mg have strong tendency to adsorb into pulp fibres with increasing pH, so do not use divalent metals as your method to measure washing efficiency will show high removal, even with no washing
- lignin is insoluble under acid conditions, so do not use removal of organics to measure efficiency
- sodium can adsorb into pulp fibres, so can be used, but may give high efficiency values
- chloride is best - it has very low interaction with pulp fibres, and is what you actually want to remove in the washer
- Displacement ratio on Eo washer shows very little difference for Na, TDS, and lignin, all around 0.85 displacement ratio
- organics are soluble, so can be used to measure washing efficiency
- the concentration of soluble Na is much higher, so can be used
- divalent metals not significantly soluble, so do not use divalent metals
- Northwood experience in measuring washing efficiency
- 2 bleach plants: same sequence - DEOPDEPD upflow
- tried chloride on Do as a measure of efficiency, but it did not work because of recycle to dilution, so used dissolved solids (Marco - dissolved solids may not all be detrimental to following stages, so may not be best test)
- decided to use displacement ratio using dissolved solids - tedious since must evaporate filtrate down to dry solids, so hired Co-op student for 4 months to do nothing but displacement ratios
- Displacement ratio as % for both A and B bleach plants of (average of 3 tests)
- Do A/B 64/28
- E1 A/B 37/64
- D1 A/B 66/32
- E2 A/B 86/93
- D2 A/B 89/96
- important variables
- vat level (poor efficiency if low)
- air entrainment in vat 1.2% (1.0 - 2.0%) noted poor efficiency above 1.5%
- costs related to chemical wastage due to carryover
- no shower flow measurement, so no dilution factor calculated
- Conclusions
- will continue to optimize the lower efficiency vats
- will provide increased operator training
- will reactivate vat level control
- will get ultrasonic flowmeter to measure shower flows
- Questions - LaValley showers, Northwood doesn’t use defoamers in bleach plant
- Weyerhauser, Kamloops experience
- evaluated Do and Eop stages to measure impact of changes
- visual examination very important
- run washer as low as possible for maximum consistency
- set showers for maximum rate
- minimize air to air doctors to keep sheet from breaking
- watch for filtrate re-wetting
- look at wire condition
- Do stage
- sample sheet, measure consistency, measure sheet filtrate pH, titrate with NaOH to 10.5 pH, ensure you compare at same bleaching conditions and throughput
- evaluated before and after shower bar change
- lower carryover with new shower bars, so can run with lower shower flow and improve consistency
- try it!!!
- graph shows came way down in caustic usage for reduced shower flow
- Eop stage
- sample sheet, measure consistency, determine liquid KNo, ensure at same conditions
- liquid Knumber is not as good a test as the Do test, but worth trying
- graph shows large scatter
- Remedies
- replace whistle nozzles with spoon type that disturb the sheet less
- keep washer wires in good repair
- review wire mesh size
- consider anti-rewet deck on washer (high cost, but may be able to justify this)
- Weyerhauser - Grande Prairie
- Do washer study - replacing washer drum, so wanted to know how much increase in efficiency would result with new drum (this data for existing drum)
- attempted to quantify Do washer performance
- neither TDS nor Ca provided an accurate basis for determining displacement ratio
- chloride concentration was found to be a good indicator to determine the displacement ratio eg. DR = 62, 45, 68, 71% on four trials, which is lower than would be expected for the new drum
- Mill X
- two similar bleach plants, but very different kappa number of filtrate in Eop
Line 1 Line 2
- Kappa No pulp 5 5
- Kappa No filtrate 1.5 5
- Total Kappa 6.5 10
- this explains the high D1 chemical consumption in line 2
- old drum washer with lots of re-wetting on line 2 Eop. Mill is working with vendor to make improvements
- Bill Miller (Ingersoll Rand at TAPPI round table)
- Effect of Dc Washing on Chemical Consumption and Eo Brightness
- Increased D1 and Eo shower flow to Dc stage significantly, resulted in 40% reduction in caustic, increased Eo stage brightness
- Three mills tried a number of tests to measure efficiency, including conductivity, Na, Cl, TDS. Resulted in very variable results
- Conclusions
- potential for saving a lot of money
- worth trying some efficiency measurements
- What can be done? What are people doing?
- install high efficiency end valves
- add satellite seal tanks to increase air removal (want about 3 minutes for vacuum drums or follow vendor recommendations)
- install new shower bars, replace whistle type with spoon type showers
- install anti-rewetting drums
- increase number of shower bars
- add vacuum assists
- wire mesh changes
- avoid shower water falling into vat
- replace water doctors with air doctors
- add press rolls (new control methods may help operation)
- automatic vat level control
- get washer discharge consistency up
- add CO2 on last brownstock washer
- change filtrate recycle scheme (are you adding dirtier water)
- baffle filtrate tanks
- ensure drop-leg configuration and diameter is proper
- do not over add chemicals
- with diffusion washers, have stroking times compatible with pulp production rates
- install baffles over vat inlet pipes for good even distribution of pulp over the drum (are they still there?)
- NOTE - different wood species have different washing performance
- Are many mills using vacuum assist? Gold River does, and finds excellent washing efficiencies, high consistency (16% consistency E2 stage after chemical addition), 0.8-0.9 displacement ratios, mill really likes them;
- On upflow towers is there a problem with air entrainment? Elk Falls has problems drawing in air at W15, so need to add defoamer. Add level control? Northwood took it off B bleach plant because of plugging. Northwood found no difference between swirl mixer and conventional dilution to the washer in terms of air entrainment in the vat.
5. Update on Bleach Filtrate Recycle - Rogelio Vega Canovas, Champion International (see Appendix 3)
- 635 tpd pine bleach plant at Canton, NC
- chloride removal process (CRP)
- started Sep/95
- precipitator ash diluted, evaporated, saltcake filter, purge brine solution
- built to remove 120 tpd ash, currently at about 100 tpd
- satisfactory chloride, potassium removal
- on-going optimization
- chlorides in WL dropped from 3.2 gpl to 1.7 gpl. When recycle process starts up this will increase again, but hopefully not above the 3.2 gpl level (for comparison, mills on coast run about 30 gpl chloride)
- metal removal process (MRP)
- fibre strainer, sand filters, softeners (ion exchange)
- normally achieve design throughput
- metals removal efficiency >90%
- high media (sand) filter on-line time
- some significant mechanical difficulties
- trace metals decreasing, especially potassium
- Filtrate Recycle
- D1 stage open
- Eop stage 20-40% closed
- no impact on bleaching
- filtrate recycle is a challenge
- Next steps
- achieve consistent MRP operation for prolonged periods of time
- complete Eop stage closure by May, while learning to balance filtrates
- complete D1 stage closure by July
- Full bleach plant closure hopefully by the Committee visit in the fall